THE MK1 MR2 2L TURBO PROJECT -
3S-GTE
Foreword:-
Having owned my MK1 for 5 years and already having modified it in quite a few
ways, I was getting a bit bored with the performance. Now MK1 MR2's are anything
but boring and even in this day and age manage to beat off a lot of the modern
stuff designed to replace it. However I've always been one for owning one-off
cars, something a little special that stands out and not only do I want to
create a MK1 that really looks the part, but one that will have the Subaru boys
demanding refunds because a 17 year old “hair dressers car” has disappeared into
the horizon leaving it choking on tyre smoke. Not that I'm a speed freak, far
from it, I just love my MR2 and want to make it unique. In the forum where this
engine swap is discussed the car is referred to as a MK1.5, halfway between a
MK1 and 2.
To the best of my knowledge there are 6 of these conversions in the world, 4
in the States,1 in Germany, and 1 in Australia, so mine will be the first in the
UK. I have 3 people here in the UK who have everything they need to do the swap
themselves but are waiting for me to complete mine so they can learn from my
mistakes and also have someone to ask for advice when there's a problem. This
hasn’t been a “lets just do it” job, I've been collecting data from around the
world for the last six months, including pictures of everything , numerous
articles, wiring diagrams and even video footage of the install.
So why this engine?…well, basically the 3s-gte kicks out 200-240 bhp -
depending on what generation you get - in standard form, making it better than
the most tuned 4a-ge. Other issues like uprating the brakes and suspension will
be tackled once the engine is completed.
Preparation:-
Originally I prepared myself for not being able to get a 3s-gte engine as
crash damaged MK2 turbos are a rare thing, so I was going for the little brother
non-turbo 3s-ge instead with plans to stick a turbo on it when the time was
right. I found a 1987 Toyota Celica for sale at the top of my street and bought
it for £80. It was an MOT failure but had a sound engine and gearbox. After a
weekend of breaking the car and having got the engine out I suddenly realized I
had made a huge mistake….this car is front wheel drive!! The gear box was no
good as the linkages are on the wrong side! How could I be so stupid? I just
presumed that it would be the same…wrong. Not to be undone I simply wanted
a MK2 MR2 gearbox that would mate straight onto the 3s-ge. I found a guy
in Newcastle who was breaking one and he said “do you want a turbo or non turbo
box?”…I said “oh, you have a turbo for breaking??”… after 5 minutes I had bought
the complete 3s-gte engine, gearbox, wiring, ecu…basically the whole rear end
from a MK2 turbo that had a crash damaged front for a silly price of £250
delivered. Anyone wanting to do this swap can expect to pay nearly £1000 for
this engine/box alone so I was very lucky. Update 29 09 02 -
At the time I didn't know the exact generation of my engine as there were 3,
ranging from 200 bhp 1st generation to 245 bhp 3rd generation. I've just been
informed that it's a 2nd generation ceramic turbo producing 225bhp and 200lbs/ft
of torque. To mate the gearbox to the hubs of a MK1 requires MK1
Supercharger driveshafts, now if you plan to do this on a supercharger then you
are one step ahead…I was not and it took me 3 months to find some and even when
I did they cost me £150 second hand, these were harder to find than the entire
engine. The SC short shaft bolts straight onto the turbo box and fits the hub,
as SC and NA hubs are the same. On the drivers side the turbo output shaft is
kept and the SC outer CV joint is removed and fitted onto the short turbo
driveshaft, this in effect gives you two passenger side SC driveshafts.There are
other things to buy or make, Like exhaust system and engine mounts but I have
95% of what's needed.
MAJOR NEWS - 15/12/02 - I've just been
informed that the front driveshafts from a Celica 4WD are identical to the short
SC driveshaft having the same outer and inner joints and are a straight no
modification option for the swap. This information is also priceless for you SC
owners looking for a replacement shaft.
Here's the 3s-gte just after delivery.
Now that’s a big lump of power! Believe it or not that engine fits in a MK1 bay
with about an inch at the back and 2 inches at the front for turbo clearance,
needless to say extra heat shields will be fabricated, and an extraction fan
fitted to the underside of the engine lid to suck the heat out. Note where the
alternator is on the MK2. This will be moved to the top right as later
described. The engine will be dummy fitted as you see it here to make everything
fit and to fabricate engine mounts. It will then be removed for engine bay
painting and a stripdown of the engine for overhaul and painting.
Here's the turbo shafts minus outer CV joints, you need SC shafts for their
outer CVs, the short SC shaft is identical to these so just use it as it is,
take the outer CV off the long SC shaft and fit it to one of these turbo shafts.
Friday 13th!!! September 2002:
In typical MR2 style it knew what was going to happen to it, and on my last
journey to work in B709 XHW for its big conversion, it decided to blow its head
gasket. Now after 5 years relatively fault free driving and on Friday 13th this
is a bit spooky.
The car had an (LPG) gas conversion fitted to it - see http://www.mr2mk1club.com/LPG.html
and the first job was to remove this completely as the 3s-gte will not run on
gas, and even if it did the kit is too heavy for the planned project. Over the
next week the work will consist of removing the old engine and gearbox,
driveshafts, removing the all engine wiring, removing the coilpack, plumbing and
fuel lines, and grinding the original engine mounts off the chassis legs. The
battery tray will also be removed for relocation to the front compartment, as
you can guess as much space as possible is needed in the engine bay and the
battery takes up a lot of it.
The MK2 alternator position causes a few problems, it fouls on the o/s
suspension mount, others have cut a notch into this for it to recess into as
above, but I had a better idea. Remember I bought an '87 Celica? Well the
Celica's alternator position is on top of the engine instead on a different
bracket so I've used this with the Celica alternator, no need to cut anything.
Here's the new alternator position, intercooler piping from the turbo will
clear above it, but intercooler piping from the throttle body does foul on the
new engine lifting hook position that will be removed after the engine is
fitted. A big bonus of doing it this way is the original alternator bracket is a
huge piece of cast iron that weighs a ton, so there's been a weight saving too.
Also I've now fitted the Celica power steering bracket where the alternator used
to be in case I fancy fitting a little bit of power assistance to my steering,
which is quite heavy due to the 17” alloys.
I will have to decide this later on as I don’t want to mess the cars handling
up, but for now having the bracket there gives me the choice. Here's the PS
bracket just above the output shaft bolts. If I do go ahead I will be using the
Celica power steering pump and rack modified to fit, and I will experiment with
different sized pulleys to just give it an assisted feel, nothing more though as
the MK1 feels sharp and precise and fitting PS might make it vague on the road.
It can always be removed if it's one of my worse ideas. You can just see the
crank pulley in this pic, this will be swapped for the Celica pulley that has a
smaller inner pulley to make the PS less effective than with the MK2 pulley. I
just want to take the heavy edge off the steering at low speeds. Either this or
go back to 15” wheels.
Monday 16th September:-
Today the project started in earnest, the rest of the gas kit was removed and
the old 4age engine and gearbox was dropped out in a personal best time of 2
hrs. I cannot stress enough how important it is to have the car properly
supported when doing this as you need to get the car right up in the air to get
the engine out from behind.
Here it is removed, note I had a bit of an oil spill! Er.. someone forgot the
oil cooler pipes…didn’t they Paul….lets say no more about that!
So with the engine out its time to get rid of all the unnecessary bits in the
bay, starting with the map sensor as this won't be needed and takes up inlet
manifold clearance space.
Next to go was the oil cooler, it was removed at its base on the rubber
radiator hosing right to and including the filler point. After that the coilpack
and that heat extraction fan are removed…the fan may or not be replaced later on
depending on what intercooler placement I go for…note that the MK2 intercooler
goes in this spot but that’s on a MK2 and it doesn’t fit in the MK1, so a
smaller intercooler may be fitted in this place, if the intercooler is to go
where an SC intercooler goes (above the gearbox) then the airflow meter and
induction kit will fit where this fan used to go and get all its air from the
vent.
See the hole left by the fan is the perfect size for the induction filter to
poke into. The next job was to remove the battery tray, two spot welds on the
top and chiselled off the engine mount. Mine came off very easily as it was
quite rotten, the new battery tray will be in the front compartment. It will be
earthed in there as well with the positive lead going up the tunnel to the rear.
Now it's time for some serious drilling, air chiselling and grinding… the point
of no return!.. off with the engine mounts!
.... this took about an hour and a half and was a total nightmare, but it
looked good when all was ground off both sides.
Here's both sides stripped down and cleaned ready for new engine mounts to be
fabricated and welded in, this can't be done accurately until the engine is in
place. The new mounts will be made from 5mm steel plates but initially made from
cardboard templates to get the basic shape then transferred to plywood and then
cut from steel. This will ensure no mistakes are made and I’ll keep these
templates and email them to others wanting to do the swap.. that is if there's
anyone else mental enough to do all this!
After the engine is initially fitted and everything lines up it will be
removed, the engine bay will be steam cleaned and painted. At the same time
aluminium heat shields will be placed along the bulkhead especially around the
turbo as there's not a lot of clearance. In fact the biggest problem with this
swap long term is heat build up in the bay and I've talked to the guys who have
done this job already and they suggest extraction fans and an air scoop under
the car to blow air onto the exhaust/turbo area to help vent it, also more vents
in the engine cover will be made to help with this.
Here's the engine lined up with the back of the car ready to be pushed under,
as you can see it's on a trolley that was made specially for this, there is no
way you could move this big engine on the floor and still be safe. I've had to
chop my existing rear bodykit spoiler away for clearance and as I'm changing
this anyway it didn’t matter. The car had a 3 ton trolley jack under the
bulkhead chassis member with large chocks of wood going from sill to sill to
spread the load, also two heavy duty axle stands are placed under to make
everything as safe as possible. In the second pic you can see I've had to remove
the inlet manifold to get the engine under, this will be immediately refitted
when the engine is in the bay as it's crucial to have everything in situ to
decide clearance and engine mount positions. In the picture below you can see
the big problem…the bottom of the engine bay is very narrow compared to the top,
but even taking this into consideration it’s a tight fit, there's just no way
that engine would go in like this with the inlet manifold on as it adds about
another 7 inches to the width.
Tuesday 17th September:-
Today was going to be a big day, it was time for the dummy fit of the engine
in the MK1 bay, now I've only ever seen pics of this done from America and as I
started to lower the car onto the engine I began to wonder if I had been the
butt of some huge transatlantic joke…” yeah let's tell this guy it fits and we
will paste some 3s-gte pics into our bays for a laugh!” …well that’s what was
going through my mind…the engine fit is that tight I was wondering if my body
shell was different from a USA model etc…..anyway I can assure you it does fit
although things are a lot tighter than I expected.
You can see here as the car is being lowered onto the engine just how close
it is… and this is with the inlet manifold removed!…as things got tighter I also
removed the n/s and o/s engine mounts for better clearance. As it approached the
top I added the inlet manifold to get an idea on clearance and as you can see
part of the bonnet catch is stopping the engine from sitting back against the
bulkhead, it needs to be as close to the rear as possible for exhaust/turbo
clearance at the front.
The shaded area here was marked out for removal and then neatly ground off,
this won't affect the bonnet catch at all and will give some vital clearance.
Now with the engine right up in place I remembered reading that someone had
taken a large adjusting tool (that’s a big hammer to us) and caved the front and
rear bulkheads in on their cars, to allow more room. I'm not a big fan of this
method and I'd rather cut away the offending steel and rebuild it around the
obstruction. So that’s what I decided, now you can go for the big hammer
technique if you like but my reasons for cutting out a section of boot bulkhead
means that I can build a removable panel that will give me access to the rear of
the engine should I need it. Some people have just fitted the engine in the bay
without doing this and opted for large heatshields on the front bulkhead but as
you can see it looks too close for comfort. Note that the engine will actually
fit without either method but its tight.
So this area was marked out and removed, it gives the inlet manifold a good
area to recess into, not a lot, but enough to make the exhaust clearance at the
front happier. I'm also very pleased with the new access I have. The bulkhead
around this hole will be reinforced with bracing so I haven’t lost any of the
strength and a panel will be fabricated from either steel or thick aluminum that
can be unbolted for access if need be. The new panel should intrude into the
boot by about 1.5 inches more than standard.
This is the engine in the perfect position, as you can see the inlet manifold
is parallel with the rear panel and because of the bulkhead modification it
allows a 2 inch gap at the front. There's a large bulge in the front bulkhead
opposite the exhaust manifold and when I take the engine out for painting this
will get slightly inverted for even more room (hammer technique again).Together
with adequate heat shields at this point it should be fine. Something that
didn’t go to plan today was my idea for routing the airflow meter and induction
filter into the fan hole on the drivers side, I cannot now do this on my engine
as the turbo pipes would need major altering to allow space so I will have to
decide where that’s going at a later date, for now I think the fan will be going
back into its place for good heat extraction.
With the engine in the perfect place I tried fitting the driveshafts and they
slotted right into place with no problems. To help with this bear in mind that
the shafts get longer as the suspension rises so as long as the shafts fit
initially with no weight on the rear wheels then they will work as they only
extend in their inner joints as the weight does go on the rear wheels. I'm more
than happy to provide accurate measurements from one point to another should
anyone need them so that their swap will be more straightforward.
Here you can see both shafts in place, the n/s shaft went right in… I had to
remove the top strut bolt and pivot the strut out a little to give space for the
o/s shaft. Overall the shafts do ultimately decide engine position from side to
side, there isn’t much free play at all.
The day ended with the first engine mount bracket offered into place, this is
basically a 6 inch piece of 5mm thick angle iron that fits nicely on one side of
the engine mount and contacts the chassis leg and suspension tower in all the
right places. A captive nut will be welded to the back of this bracket when the
hole is marked through the mount. I've been advised to drill the hole 1cm higher
than it should be here to allow for the mounting rubbers taking up the weight of
the engine, so if you mark and drill 10 mm up it should fall back into the
original place…. Clever eh!…another bracket will be made for the other side of
the mount as well and this will just be welded to the chassis leg. These mounts
are over engineered and are thicker and stronger than the original MK2 mounts.
Wednesday 18th September:-
Having looked at that offside engine mounting this morning I decided it
wasn’t what I was looking for, what if I had a problem with the captive nut
coming free? There would be no access to it boxed in like that so I decided on a
different design of mount, it's actually the one that everyone else seems to go
for anyway, basically it's two straight bits of 5mm steel ether side of the
mount that’s profiled to fit the chassis leg and inner wing. So I set about
making templates for these out of card.
Heres both profiles of mounting in card, these are fairly accurate and the
right hand edge of these fits the inner wing/chassis leg very well, the hole for
the mount was also marked on these 10mm higher than the actual position to allow
rubber movement. They were then scribed onto the 5mm steel plate that I have and
then cut out using an angle grinder.
The position of the bolt hole was marked and drilled and both sections tack
welded into place ether side of the mount, all these welds have to do for now is
hold the engine, nothing more, the brackets will be very solidly welded right
round their circumference and boxed in with a square plate on top joining them
together when the engine is removed. A big tip to get the engine in the right
place prior to making this mount is to screw the driveshaft outer nuts onto the
shafts so they are flush with the end of the shaft. Then push the shaft in as
far as you can and note how far the nut travels. Do this for both sides and get
the distance travelled the same for each nut by levering the engine left or
right. I found it to be perfect when the hub covered half the nut on each side
as seen below. Now to get the height of the engine right is a matter of getting
it as high as possible with the lid shut and still clearing the manifold. Also
from underneath the car the gearbox output shaft should run parallel with the
rear chassis member and its top edge level with it.
Get this amount of travel both sides and the engine should be in the right
place left to right.
Here you can see the output shaft parallel to the chassis, note the sump is
about 1.5 inches lower than the suspension mount, so it's important to get the
engine as high up as possible. In the second pic note the badge on the inlet
manifold is parallel with the boot edge. With the offside mount tack welded I
jacked that side up 1cm and the bolt pushed through easily, then the jack was
let down on that side and the engine settled back to its original position
proving that the 1cm higher than should be hole worked a treat. I then made
templates for the nearside mount, scribed them onto the steel, cut them out and
placed them into position for welding tomorrow. There is some adjustment on the
nearside mount as the holes it is attached to on the gearbox are oval and allow
some movement. I've kept the templates I made for the mounts and these will be
scanned and emailed to anyone who wants them. Again this mount will be boxed
together with a square plate on top. Strength is the key and these mounts are
very very strong.
Thursday 19th September:-
The first job of the day was to tack weld that nearside engine mount in place
and after using the 10mm higher than is technique on the other side I was
confident it would be easy. It was and 30 minutes later the whole engine was
supported by its new mountings.
The next job was to fabricate the rear torque mount that goes on the gearbox…
it needed making from scratch using bits from the old 4a-ge mount and most of
the turbo mount plus some extra steel. Firstly an angle iron section was drilled
and fitted to the original gearbox holes, this was a bit tricky but all the
holes lined up eventually, then a little side bracket was added and welded onto
the angle iron section. Here you can see it fitted, there are two bolt holes on
the front face as well but only one bolt is fitted here, I’ll fit the other when
the engines out. Note the added bracket to get as much support as possible from
the existing mounting holes. The second pic shows the old turbo mount, as you
can see there's no room for this but the main body of it will be used. I removed
both side brackets from it leaving the centre piece only. This is the perfect
shaped bracket to be fitted upside down to clear the chassis.
Next I removed the top section from the old 4a-ge mount that would be used to
attach the turbo mount to the chassis. It was placed on top of the turbo mount
and welded on.
This enables the strong turbo mount to be attached to the chassis, using the
old 4a-ge mount just isn’t an option when there's this much power, even the
3s-ge non-turbo mount doesn’t last long. The top bracket was welded on the
opposite way to original to form a little channel for the chassis to rest into.
With all the pieces fabricated they were fitted together and it looked really
good, a small side bracket was welded onto the other side to catch an unused
hole on the gearbox, as I've said before, you can't have enough strength.
The whole mount fitted looks very strong, this doesn’t support any weight it
just controls engine flex under acceleration, again it has been over-engineered
to be on the safe side. I may add an angled piece on top of the rubber mount and
bolt it through the back of the chassis where horizontally arrowed in the
pic.The day ended with me playing with airflow meter and filter positions to
make sure it was all going to fit in nicely.
Friday 20th September:-
This project is moving along much quicker than I anticipated, it should have
taken me about a month to get this far but it just goes to show that all that
research and forward planning has paid off, I would highly recommend anyone who
is attempting this conversion to do as much homework as possible before even
thinking about cutting out engine mountings! All I can say is I take my hat off
to the first guy who ever did this in America….he's a brave man. Anyway, today
was about concentrating on finishing the rear torque mount and fabricating the
front torque mount so that by the end of the day the engine would be fully
supported by all four mounts. I started by removing the rear mount and seam
welding the whole thing up.
Here it is all done, this like all the other bits, will be shot blasted and
painted before the final refitting. Next was the front torque mount, it is made
with a combination of the old 4a-ge mount, the turbo mount and fresh steel
plates added by me. Here you can see the old mounting and the first job was to
remove the rubber mount block as we only need the bit that bolts to the
car(arrowed). The mount was cut along the yellow line to remove the block. Next
the turbo mount had all of it's brackets ground off to just leave the rubber
block as pictured. Again the arrowed piece is the only bit to be kept.
These two sections are now attached to their respective homes, the 4a-ge
bracket to the car as it would be, and the turbo rubber block to the gearbox.
Now all that remains is to join the two sections together with 5mm steel plates
either side.
Here you can see I've made templates out of card that will be the steel sides
of the mount, these too have been kept and are available for those who want
copies. The templates were scribed onto steel and cut out. These were then tack
welded into place joining both bits of mount together. Once again no sacrifice
with strength, these torque mounts do exactly that…. Stop the engine flexing
under high torque.
The whole mount was then removed and seam welded around every join and on
both sides. It was then refitted and small areas marked out on the sides (in
yellow here) for future trimming to make them clear the chassis better and to
look more rounded.
It was a fairly easy mount to make compared to the rear mount, and again
don’t even think about using the old 4a-ge or even supercharger mounting blocks,
I've been told they won't last 5 minutes. The trick is to use as much of the MK2
equipment as possible on the whole project.
Monday 23rd September:-
With the engine in place and fully supported by it's new mounts, it's time to
start fabricating that new back panel. After a lot of thought I have decided to
put my intercooler in the boot on the far right hand side. I've seen three
different intercooler placements on previous projects and I think mine might be
a good alternative. I'm using the boot because its totally separated from the
engine bay and therefore won't have any of the heat from the engine affecting
the intercooler, also I can make neat piping to this area from the engine that
won't look out of place. Thirdly the boot will have an airscoop built in above
the intercooler that will catch air coming off the roof and this will keep
things cool. Theres plenty of room for the fan in here too and I won't lose a
lot of boot space.
The pipe from turbo to intercooler was fabricated first using 2.5 inch bore
steel pipe and similar rubber piping. This is fed into the top corner of the
boot and meets the intercooler.
The neck of the IC was cut and altered to meet this pipe and will either need
welding back on or sleeved with a rubber joint (arrowed).The second pipe from IC
to throttle body was a little more complex, there is no real method to fitting
these pipes, it's more trial and error, or you may go for an entirely different
IC placement. The three I've seen so far are (1) in the SC position above the
gearbox (2) in the MK2 position using a smaller IC (deno from the USA claims hes
used the standard IC here but mine wouldn’t fit) or (3) vertically in front of
the gearbox at an angle with a scoop made to catch air rushing under the car.
Here you can see the second pipe, the only drawback with this method is it
slightly covers the oil filler cap but I can live with that for now. It helps to
have a large selection of rubber hoses and angled bits of steel tubing to make
these pipes no matter where you place the intercooler.
My biggest problem on a project is staying focused on what I'm doing and I
easily get distracted by moving to another job that needs doing rather than
sticking to the task at hand and getting it finished, this is what happened
today and I left the boot panel for another day. Instead I worked on the fuel
pump…I did a bit of research into wether or not the 4a-ge in tank fuel pump
would deliver enough fuel pressure to the 3s-gte, most people have carried out
this swap on superchargers which have a higher fuel pressure pump than the NA
and I've been told they haven’t had any problems. However there was no definite
yes or no as to the NA pump being up to the job, for those who haven’t changed a
MK1 fuel pump let me just say it’s a pig of a job, basically the whole tank has
to come off to get at it and the tank has more pipes going to it than
Middlesborough! So with already having a turbo fuel pump spare I decided to fit
it anyway to be on the safe side.
Here's the two fuel pump carriers, the 4a-ge carrier is on the left, the
turbo on the right, the inlet and outlet pipes are a different length and also
the turbo carrier is about an inch taller than the 4a-ge, however both pumps are
identical to look at sharing the same wiring and plumbing connections. You could
get away with just fitting the turbo carrier without swapping pumps as it bolts
on in the same place but the pipes do need altering. Here you can see the turbo
pump fitted to the 4a-ge carrier on the left. I happened to have a spare 4a-ge
carrier so I fitted it to this ready for the tank coming off. The tank will be
removed as soon as the engine comes back out as there is lots of pipes to
disconnect in the bay.
Thursday 26th September :-
Having looked at that intercooler to throttle body pipe, that I made
previously, made me think I'm letting standards slip in a bid to get this
project done quicker. To be honest it's crap and I never liked the way it
covered the oil filler cap so the first job today was to rethink this pipe and
get it looking how Toyota might have done it instead of me. After playing about
with various bits of tubing I found a much neater way of doing it and I think
you will agree it's much better than the previous attempt. Note that the turbo
to IC pipe changes to rubber just before the suspension strut to stop vibration.
First I removed the old pipe and scored 2 points with a well aimed shot at
the scrap bin, then fabricated a sweeping curve that bypasses the oil filler
point and exits exactly where the intercooler is. I then made a bracket from 3mm
steel to join both intercooler pipes together to make them very strong. This
will also reduce vibration and hold the pipes exactly where I want them. These
new pipes will now be shot blasted and a good friend of mine who works in a
plastic coating firm, will be plastic coating all my pipework in his lunchbreak
when the boss isn’t looking!
Next job was to return to making the rear panel in the boot. I've decided to
give the manifold a good area to recess into, so this panel will now intrude
into the boot by 2.5 inches. Before a removable panel can be made I had to
strengthen the hole that I made with 40mm angle iron, these will form the outer
shape of the new rear bulkhead and probably add more strength than was there
before I chopped it.
Above is the first piece welded in, this just comes up to the intercooler.
The area in front of the intercooler will be boxed in right up to the place
where the pipes come through. Here I plan to leave an oblong hole for the pipes
and line the edge of the hole with a rubber door seal so the pipes don’t chafe
on the body. In the second pic the next support is welded in and this square
hole will have a bolt on panel attached to it for engine access. Using stronger
steelwork than was removed means the whole area should be rigid.
Friday 27th September:-
With the strengtheners put into the boot wall I'm leaving the plating of this
area until the engine is out and I have access to both sides of it. All that
remained in the boot area was to mount the intercooler in the right place to
finalize the position of the pipework going to it. First job was to make a
support bracket to hold the IC in place and this was made from 20mm aluminium
angle that was cut and bent to the right shape, a few holes drilled in it to fit
both the IC and the rear panel and it was mounted using rubber washers between
it and the body to minimize movement.
With the IC finally in place the pipes needed positioning and marking ready
for welding. This is the only point in the entire project when I can't do the
work myself, I have a lot of welding equipment but nothing that will weld
aluminium successfully so I took the IC to a local engineering firm and 20
minutes later they used a TIG to join my IC pipes back on in their new position.
Here you can see the IC all welded and it was a perfect fit onto the engine
pipes. All that remains to do to this is spray paint and fit.
Heres the boot vent cut out above the IC, sides were then made for the vent
going down to the IC, they stopped about 10mm short of touching it so a good
rubber seal could be added to the bottom lip, much like the SC seal on the
engine lid.
You can see the sides had a 90 degree lip on the top to weld it onto the boot
lid, these welds will be ground down and the lip blended into the boot, then the
whole vent will be covered by a forward facing air scoop. I'm going for the
Imprezas scoop if I can get one but failing that I may just make one from
scratch. It will be subtle and only rise about 20mm at its highest, I only want
a little air caught here, not make a parachute out of my boot!!. The next job
was to fit a rubber door seal strip to the bottom of the vent to make it seat
onto the IC. This will help keep it firm and also keep all the air going through
the IC rather than around it. The seal fitted perfectly, there is some tidying
up to be done on the underside of the boot with seam sealer but it I'm happy
with the end result.
With this work now done there is no reason for the engine to stay in now, all
the necessary brackets have been made and everything lines up in the correct
place, so next week will see the engine out for the final time to fit a new
clutch and timing belt to it and repaint or polish the engine where necessary.
Along with this the engine bay will be detailed ready for the final install.
Tuesday 1st October:-
First job today was to remove the engine, it all came out very easily but
only with the inlet manifold removed and I really saw the benefit of the boot
panel fabrication. Next both engine mounts on the chassis had to be totally seam
welded and reinforced with more 5mm steel plates. The first of these was made
from card and transferred to steel and was welded into the top of the o/s mount
to tie the two sides of it together and welded to both the suspension strut and
inner wing. It is important to fit the rubber engine mounting block with the
bolt fully tightened while welding as the plates may “pull” when welded, this
will keep them in the right place. Also a bracing piece was added coming up from
the chassis leg and joining the bottom of the mount together. Here you can see
it all welded up and the bolt has been fitted to weld the nut captive onto the
mount. There's no way a MK2 turbo has mounts as strong as these but it's better
to be too strong rather than weak. Ok I know all this steel is extra weight but
at least you are sure the engine is stable. All that remains for this mount is a
bit of grinding to tidy it up and seam sealer along the joins like Toyota do it.
The same strengthening work was carried out on the n/s mount and again the
mounting block was fitted and fully tightened to make sure the sides didn’t pull
apart or close up.
Here you can see it seam welded with a support on top and in the second pic a
small brace is added to the underside and onto the chassis leg, again the bolt
was tightened to weld the nut captive. Both of these mounts are now finished and
ready for painting. With the engine out its time to start stripping it for
inspection, new timing belt and a fresh clutch kit and paint it up. Various bits
will be polished or chromed before refitting.
A point to remember is to keep the turbo pipes covered at all times to stop
dirt or anything else falling in. Both gearbox oil and engine oil/filter will be
changed here too.
Wednesday 2nd October:-
With the engine out it was easy to indent the front bulkhead around the turbo
and exhaust area, this need'nt necessarily be done as others have left it alone
and taken the risk but I know this area will get hot and for peace of mind I'd
rather have as much space as possible between the exhaust and bulkhead. A large
hammer was used to recess this area which will have a good heat shield over it.
On inspecting the timing belt and pulleys I found the bottom idler pulley
(arrowed) to have a slight noise on it and it’s a nasty job to do when the
engine is in so I'm replacing it now. The engine block and cam cover were
treated to a fresh coat of paint in the same shade as the plastic coating I'm
having done on the pipework. Also I inspected the clutch and its worn right down
to its rivets so it’s a good job I checked it. When swapping any engine it's
always a good idea to presume the timing belt, it's pulleys, and the clutch are
faulty as these often get neglected…what can I say…these MK2 owners just don’t
know how to look after their cars!!!
The 2nd pic shows a shiny rivet on the friction plate, this clutch would
definitely slipped had I used it. The clutch kit is going to cost you around
£125 plus vat, timing belt around £25 and that idler pulley for me is an extra
cost of £45
Monday 7th October:-
I've had a lot of trouble trying to find a clutch kit for a MK2 turbo, not as
easy as you would think…. Plenty available for the non turbo at about £80, but
the cheapest I could find for a turbo version was over £230 with the vat. So
after many phone calls to people in the know it was suggested I try to find a
clutch for the Celica turbo as it should be the same. The next day I found one
at parts suppliers Langley Tyre and Auto who supplied one at £135 all in. After
a quick check it's identical to the MK2 turbo clutch and the only difference I
could find was the spring clip on the release bearing was a different shape so I
just used the old clip on the new bearing, doing this will save you over a
hundred quid on the clutch cost. With the clutch rebuilt and nearly a week of
engine detailing done its starting to look the part although there's lots more
to be done.
I got all of the pipework back from the plastic coaters and they look
fantastic (cheers Anth), well worth doing and of course will never corrode. Note
that the prettier the engine gets the worse my garage floor gets! The turbo
outlet was polished up and although it took all day it was worth it, so the
engine is now finally ready to go back in safe in the knowledge I won't have
timing belt or clutch worries. I've also sourced a set of blue Samco coolant
hoses for a MK2 turbo that will need very little modifying to fit the MK1. Next
job was to finish off the engine bay rear wall section. I started out by making
a panel for the offside and welding it in, I used 2mm steel here - instead of
the 1mm stuff used on body panels - for strength. I've left a hole at the top
for the intercooler pipes to run through and the whole edge of this has been
doubled back to form a lip that the pipes can't chafe on.
Here's both side sections welded and with only the bottom chassis to repair
it all looks nice and strong. With the whole thing fabricated and seam sealed
the engine bay is nearly ready for cleaning and painting. I will be using stone
chip first on the engine bay to give it a tougher texture, and it forgives
grinding marks and scratches well.
Just a removable hatch to make for the square hole and this area is finished,
I'm going to make this out of thick aluminium checker plate with a rubber seal
around its edge and bolts screwed into speed clips for the fastenings.
Tuesday 8th October:-
The main job today was to get the fuel tank off and replace the NA fuel pump
with the 3s-gte turbo item, this will ensure you get the correct fuel pressure
and will supply all the fuel the engine needs even if it is modified. I already
have plans to turn the boost up from a standard 10psi to around 15psi and the
turbo pump will be adequate for this. A few weeks back I already fitted the
turbo pump to a MK1 carrier so it's just a matter of dropping the tank off and
swapping the pump carrier. To get the tank off isn’t easy and the full handbrake
linkages have to be removed with all it's brackets. Then all the filler pipes
and breathers in the engine bay have to be removed as well.
In the first pic I've removed the linkages and placed them to one side, all
that holds the tank now is two supporting straps, give the nuts on these a spray
with penetrating oil beforehand cos if these snap it would be a very difficult
job to replace them. All nuts and bolts underneath MK1s are prone to snapping
off so luckily all mine came free. It goes without saying that there should be
no petrol left in the tank here for safety reasons and an empty tank is easy to
refit. In the second pic the breathers have been removed with just the filler
pipe to go. The tank was supported by a trolley jack and gently lowered. For
some unknown reason my tank didn’t have the proper electrical blocks on top of
it going to the sender unit and fuel pump…and I had to cut the wiring to get the
tank off, looks like a previous owner must have had the tank off before and did
a bodge job. It took 2 minutes to change the pumps over and I soldered a 3 pin
block connector into the sender unit wiring and a 2 pin block connector into the
pump wiring so that future removal will be as it should be (arrowed).
The second pic shows the tank ready for refitting, it went back in a lot
easier with the new wiring. The only other job to be done today was stonechip
the engine bay over all the walls and fabricated sections, it's nearly ready for
painting
Wednesday 9th October:-
I managed to source a large offcut of aluminium sheet from a local machine
shop and made a large template out of card to make the front firewall
heatshield. Care was taken to cut out all of the necessary access holes for
water pipes and the brake servo pipe and the whole shield was pop riveted onto
the bulkhead, it not only looks the part but will provide critical protection
from the heat radiated from the exhaust manifold and turbo.
I may make extra thicker shields to go right were the turbo area is to be on
the safe side, but I think this one should be adequate for now and certainly
it's more than others have done in the same area. Note in this pic I've cut a
large area out of a spare engine lid that I had, this is going to get a bulge
fitted to it with a vent facing back to allow the extra heat generated by this
engine out the rear. The extra space above the engine will also allow me to fit
a much needed strut brace between the suspension tops, something that I've yet
to see on a 3s-gte conversion due to the lack of space between engine and lid.
For information you don’t have to cut the lid, the engine will fit under the
standard lid without modification, it's just personal preference. I've also
painted the servo pipe and refitted it.
I've tried for weeks now to find a decent air scoop to fit over my
intercooler vent on the boot lid, but nothing looked good enough or was simply
to big and clumsy looking so I decided to make mine from scratch. I started by
using 10mm diameter round bar to make the vent hole at the front and flat bar
welded to this to make a framework for the scoop.
A steel cover was then made with 1mm sheet steel cut and folded to the
perfect profile. Next silicone was applied to the top of the framework to bond
the top of the scoop onto the frame, this could be drilled and spot welded but
I've found stuff like this tends to warp easily with the heat on a flat surface.
The scoop was then tack welded around its base and when the silicone cures the
scoop will be blended into the bodywork. All that’s left to do to it is fit a
mesh front after the car is painted. Hopefully this will catch air coming off
the roof and cool the IC.
Thursday 10th October:-
With the intercooler scoop fitted attention turned to the bonnet bulge that
doubles as a heat vent and leaves space for the strut brace. In the same fashion
as the IC vent a frame was made with 10mm bar at the front and flat bar on the
rest. I only want these vents to be subtle and when blended into the body they
should be just that. The second pic shows cross bracing that will have the
silicone sealant on it to stop the panel flexing. Further strengthening supports
were added to the sides and to the catch area.
Again a hood was made for this vent and this time I've chosen to place a few
spot welds on the top to help keep its shape as this is much larger than the IC
scoop. It's important to only spot weld metal this thin as a solid seam weld
will distort the whole panel. I usually keep the spots about an inch apart and
as you can see its all stayed in shape. One thing I've wondered is does the SC
bonnet with its higher vents give enough clearance for a strut brace (with
3s-gte fitted) without modifying like I've done?
These pics show both scoops fabricated and their mesh fronts fitted (mesh
stolen from a large piece left in the yard by a Mr Michael Sheavills that is
being fitted to the Northeast Track Day Car,
hey if it's left lying around I’ll use it!!!), Michael has also donated an
excellent MK2 Jasma rear exhaust silencer to the project which will be covered
later so many thanks to him. I believe no one else has fitted these vents with
the 3s-gte swap but I think they are very much needed in such a small engine
bay. If you are intending to do this project then its really up to you, with a
different intercooler position then that scoop isn’t needed but I would at least
recommend the engine lid vent if for nothing else other than being able to fit
the strut brace. It's worth bearing in mind this engine is 80kg heavier than the
4a-ge and produces 225bhp with 200lbs/ft of torque so a strut brace is a must.
All that remains for these vents is to be tidied up and blended into the body
with a small amount of bodyfiller and a good high build primer. As far as the
3s-gte project goes this is as much as I will cover in this article about
bodywork on the car, it's already cosmetically different on the front end - see
Front End Mod - and
there are more body mods to be made on the rest of the car that won't be covered
here.
Wednesday 16th October:-
After a few days of preparation on the engine bay it was finally ready for
painting and although not perfect I'm quite happy with it, let's just say it’s a
lot better than it was!
As this car is unique (or one of very few) I decided it needed a non standard
paint colour to make it different from the rest. I've always been keen on yellow
but only a certain shade that’s also found on Porsche boxters and is also an old
MG midget colour, it’s a pastel yellow called “pale primrose” that really stands
out without being hard on the eye. It's very much a matter of personal taste and
you either love a colour or hate it. I also wanted a colour that would be in
sharp contrast to the blue engine detailing to make the engine stand out . With
the engine bay masked up in all the right places I applied 3 coats of 2 pack
paint to the bay.
I took this opportunity to stand in the engine bay and get some paint onto
the inside of the roof posts which has always been a very hard area to paint on
MK1s, you really need to be double jointed to paint this area! With the paint
applied and allowed to dry I masked the lower half of the bay from the chassis
legs down and applied 2 coats of black stonechip, this will help protect the
underside and also blends the underseal into the bay.
With the whole bay painted and demasked it really looked good against the
aluminium firewall, all that remains to do here is tidy up the gear change
cables and refit a freshly painted extractor fan and refit the fusebox. The bay
is now ready for the final engine fitting which I know will now fit perfectly
because of the dummy fit a few weeks ago, it's all coming together now.
Thursday 17th October:-
Today saw the engine going back in for the final fitting, lots of care was
taken not to scratch any of the new paintwork on the bay or engine, after an
hour it was in and everything lined up exactly as it had done before. The inlet
manifold was again left off for the refit to give more clearance. The
driveshafts were then connected up and both torque mounts fitted, it's just like
putting a 3s-gte into a MK2 now as all the hard work has been done. Indenting
the front bulkhead and removing a section of the rear has really paid off, I now
have a good 2 inches of clearance between the exhaust manifold and wall and at
least 3 inches clearance between the turbo and wall, still not an awful lot but
together with the aluminium heat shield I expect it to be fine. Note again that
vitally the hoses to the turbo have been blanked off to stop anything falling
in.
The second pic shows it in with various bits refitted, the inlet manifold
wont be fitted until I'm ready to fit the wiring harness as it threads through
between manifold and head as it connects up to different
sensors/injectors/ignition components.
With the main mechanical stuff done its time to start plumbing it all in,
most of this is fairly easy as it connects up roughly where it would on a MK2. I
sourced a set of blue Samco performance hoses from a very helpful MK2 turbo
owner on the drivers club website (cheers Mark). Next I made a small pipe with a
bracket welded to it, this is to join the drivers side radiator hose to the o/s
engine hose.
Here's the first piece from engine to pipe and in the second pic the pipe to
car hose is fitted, you could just make a one piece pipe going straight to the
car from the engine but I wanted a bracket that would keep the hosing secured to
the bulkhead away from the heat source. The bracket will now be bolted on with a
rubber washer between it and the aluminium. Even with this bracket the hose is
about 2 inches away from the factory heat shield on the exhaust, this should be
fine but to be on the safe side I'm going to pop rivet a small aluminium shield
around the hose where arrowed.
Friday 18th October:-
The radiator hose on the left side was very easy to fit with no altering
needed at all and there's plenty of clearance between it and exhaust manifold.
The fuel return pipe was also connected and this too is a straight fit, I used
the pipe from the MK2 that was already on the engine and it fits perfectly onto
the fixed steel pipe on the bulkhead (arrowed).
As there's no standard airbox fitted to the engine, the air flow meter (AFM)
is unsupported so a few brackets need to be made to hold it steady. Here you can
see I've made a support that’s bolted to the engine mount holes that are
normally used for a small damper that’s fitted to the MK2’s. I've yet to work
out the function of this damper, it looks like an anti-roll bar drop link with a
rubber bush at one end and it seems to control lateral left to right movement
but my engine is absolutely solid on its mountings so I don’t see the need for
it. Either way I've never seen anyone else fit this so I’ll leave it off and
maybe fit it at a later date if found to be necessary. This AFM support is
welded to an existing steel bracket on the back of the unit. It must be
remembered , that when mounting anything onto the engine, not to attach any part
of it to the body of the car unless rubber is used in between. The vibration of
the engine will simply snap it off or cause other damage.
Above I've fitted the filler point, I've used the MK1 filler and modified it
to fit, first I removed all of the plastic brackets from it and then I've
blocked one end of it off, like MK2’s are, with a thermo switch. It just
happened that the switch was the right diameter to fit the end and also I plan
to run a heat extraction fan off this. There is no need to do this you can
simply use the MK2 filler neck instead. You can also see I've fitted the MK2
expansion bottle next to the air filter, it recesses nicely into that curve in
the bay but the neck is 6 inches too long so this was chopped down and plastic
welded back on where arrowed. Again Samco hoses are used on the filler point and
overflow tubing.
Monday 21st October:-
Some things on the engine connect very easily, others need a bit of
modifying, and I'm pleased that Toyota made the gearbox speedo drives the same
on the 3s-gte and the 4a-ge. The cable screwed on perfectly and the gear change
cables also fitted as if they were being fitted to the original linkages. The
heat extraction fan was also refitted after painting, this will be wired up
through the original MK1 air temperature sensor that’s mounted above the exhaust
manifold on the 4a-ge, I’ll have to play with its position on the 3s-gte to get
it switching correctly. The clutch slave cylinder flexi pipe was also connected
using the flexi from the MK2, the MK1 flexi is no use here as it has two female
ends on it and the MK2 has a male and a female.
Here you can see it fitted, note I've bent the bracket slightly to allow a
little more free play. The engine is now plumbed in, fuel lines connected,
clutch and gear cables done and all the little ancillaries fitted around the
engine, now it's time for the serious fun to begin….wiring. In my opinion this
is probably the hardest part of the swap, it's very easy to wire it up so that
the engine actually runs, just power up the ECU and Circuit open relay and it’ll
run, but there's more to it than that, there's dash instruments to get working
like RPM, oil pressure, water temp and also the engine warning light. The first
thing to do was fit the engine side of the harness to the engine, this is
relatively straight forward and everything connects where it should. I then
routed the harness through the original hole in the rear wall together with the
MK1 wiring that comes from the dash and fusebox. It's in the boot where all the
vital connections are going to be made. It's vital that you have year relevant
full wiring diagrams of both AW11 and SW20 (turbo), I can provide these via
email if you need them. For now the engine work is finished with only the
exhaust system to fabricate. All of the IC piping was refitted and IC refitted
under its new vent.
Final job of the day was to fabricate a new battery tray in the front
compartment. It was made from 40mm angle iron and situates the battery in the
corner of the bay. You can put it wherever you want but I like this position as
it also allows me to carry a space saver spare wheel beside it. The battery will
be earthed here and a thick positive cable will run up the tunnel and onto the
starter motor.
Tuesday 29th October:-
There's a lot of connections to be made to wire it all up and I strongly
recommend every single connection is soldered and shrink wrapped, or at the very
least insulating tape on the soldered joints. With all of the MK1 engine harness
removed there should only be the large grey connector left in the boot, this is
called the N1 connector and this is where I'm wiring
my MK2 ECU and engine harness up to. Which ever Circuit Opening Relay (COR) you
use it must be wired into the N1 connector. I've used
the MK2 COR but either will do. I've also decided to retain the MK1 fuel pump
relay and just wire it up to the MK2 COR. All of this won't be understood until
you have read the wiring diagrams over and over and have become very familiar
with both wiring harnesses from both cars, a good understanding of how it works
is 90% of wiring it up correctly. I've also used the engine side of the N1 connector to wire it all up so that it can be removed in
future if need be. I've mounted the MK2 ECU near to the harness entry point and
although this all looks like a crows nest everything is labeled and ready to
join. Once its all wired it can be tidied at a later date. Here you can see each and every wire on
the N1 connector (circled) has been labeled. These
are joined to their respective wires on the MK2 harness. Here's the MK1 N1 connector showing both sides and the pin outs.
Here is a table showing the relevant
connections that have to be made from the N1 connector to the MK2 harness, please note that
these colours were correct for my 1985 NA but may be different on other years or
models. The EFI relay wire (7) is connected to the black and yellow wire on the
COR. The black and red wire coming from the Engine Main Relay (12) is connected
to the thick black and red wire on the MK2, this powers up the coilpack and live
feed to the igniter/amplifier. This would normally be connected to the
Ignition Main Relay on a MK2. The fuel pump wire (18) is connected to the blue
and black on the COR. I haven’t used all of the N1
wires as I'm wiring my cooling fans on the IC and engine bay fan onto a separate
circuit so I've got more control over heat issues. For instance if the MK1
circuitry wasn’t bringing the fans on soon enough I can alter this by moving the
air temperature sender closer to the heat source or fit a manual switch for both
or either on the dash.
Circuit
Opening Relay Connections 1 Blue wire on the COR to N1 - Pin
18 (fuel pump) 2 Black and yellow wire from all of these- TPC, T-VIS, ISC,
EGR, Ox sensor, check connector
(+B),ECU wire A12 + A13,all joined to N1 Pin 7 (EFI main
relay) 3 ECU wire A11 + M2
to Starter solenoid Wire (black and white on MK1) 4 ECU B17 5 Ground Here are the wires that come from the
Circuit Opening Relay (COR) The MK2 ECU also has additional wires
that wont be used, mainly because they have nowhere to connect to on a MK1 but
won't affect fuel metering at all. There's a blue wire with red stripe coming
from the ECU that goes to the MK2 fuel pump relay, a MK1 doesn’t have this wire
on its relay and its used on the MK2 as a low speed circuit for the pump to
operate at a lower pressure when the engine is idling or cruising. Many who have
done this conversion have opted not to use this wire (can only be used in
conjunction with MK2 fuel pump relay anyway) and just have the pump operating at
full pressure constantly just like a MK1 does. There is also an idea that during
the switch over period between low speed circuit and high speed that there's a
momentary lag in pressure so many MK2 owners disconnect this wire as a
modification. I'm now including the relevant MK2 wiring diagrams that are
priceless when doing the swap.
These electrical diagrams show all of the MK2 wiring to the ECU and are
indispensable when it comes to doing the job. I also have diagrams of the
starting and charging circuits should you need them. Please note that the
information I give about wiring is merely an account of what I've done and
although it may used as a reference I cannot take any responsibility for it
being wrong or any damage it may cause as a result, in other words…your car may
be wired differently! Please email me with any electrical queries and I’ll help
in any way I can.
Thursday 31st October:-
With nearly all of the wiring done, there only being some fans to wire up
etc, It's time to connect the throttle cable and the brake servo pipe. The
throttle cable fitted but it was a bit tight so I extended it by about 4 inches
so it wasn’t stretched over the engine. I did this by extending the outer cable
and threading a new length of inner cable through it and then crimping the
proper ends onto it to make it a perfect fit, it works very well and feels light
while getting 99% of full throttle. I don’t like getting 100% as it means the
cable is then under tension and may snap over time, there is also some
adjustment available on the throttle body just like the MK1.
The 2nd pic although not very clear shows a vacuum T-piece I've fitted to a
hose coming from the inlet manifold (arrowed), this will be routed by means of
brake pipe under the car and to the dash for my turbo pressure gauge. With the
wheels back on the car was lowered back to earth for the first time with its new
engine in and as you can see by the wheel arch clearance the extra weight hasn’t
really affected the ride height , I'd say its maybe 5mm lower than before.
The shot under car shows the amount of ground clearance I have, it's not much
more than the 4a-ge had and there's a good 4 or 5 inches to the lowest point
being the exhaust downpipe that I've just fitted here ready for the system to be
made. All I've been able to use from the MK2 system is the downpipe and flexi
joint (arrowed), from here various bends will be tack welded into place and onto
the Jasma rear silencer that will sit neatly where the 4a-ge silencer used to
go. I'm also fitting aluminium checker plate to the boot floor to keep heat away
from the boot, after all my intercooler is in there!!!
The only job that’s needed in the cabin is to fit the turbo pressure gauge to
the dash, I've chosen to mount it just above the wiper switch where its easily
seen. Two wires on it go to the + and – on the clock illumination and the vacuum
hose connects to the inlet manifold via a long piece of brake pipe secured along
the tunnel.
Here is the Jasma rear silencer from a MK2 that was kindly donated by Michael
Sheavills, it's just a matter of supporting it in place with axle stands and
tack welding 2.5 inch tubing from the downpipe, under the crossmember, and sweep
it into the box, then remove the whole thing and weld it solid. Refit and weld
some hanger brackets onto it making sure it isn’t fouling anywhere even when
moved a lot.
Today sees the end of the article, everything has been done bar a few bits of
tidying up. In the next week or so I’ll be turning the key for the first time
and I’ll conclude this then with an update on how it runs and any further
problems encountered. For now the car will still be undergoing its bodywork so
it will be some time before it hits the road, or with the addition of wings,
runway! This article was written so that I could give back what so many have
given me by way of information, help and in some cases parts. I hope it proves
useful to some other nutcase out there who wants to break the sound barrier.
Sincere thanks must go to Richard Morgan of the MR2 MK1 Club and MR2
Supercharger.com who has tirelessly edited and updated this article and never
complained about me clogging his email with big files, without him it just
wouldn’t have been possible. So that’s it! Fensport and MR2 solutions have
acknowledged that it’s the first 3s-gte powered MK1 MR2 in the UK, also a big
thanks to all the lads in America for their help (Deno,Alex and Warren). Please
feel free to email with anything you need help with, Paul Woods.
With everything checked and double checked the key was turned for the first
time, all of the instrument lights came on properly and the engine cranked.
Within ten seconds of cranking it slowly fired on 2 cylinders then 3 then onto 4
and ran perfectly for 5 minutes before I shut it down to check for petrol leaks
etc. The first problem I encountered was oil pressure, there wasn’t any! So I
earthed out the wire on the sender unit and sure enough the gauge went off the
scale proving that the wiring and gauge were not faulty, embarrassingly after
replacing the sender unit with another I had, it still didn’t work and after an
e-mail to Deno in the States I was reminded that a MK2 doesn’t have a gauge and
that the sender unit is merely for an oil light and therefore works on or
off…sometimes the simple things can slip past. So the MK1 sender has to be
fitted instead and as it's bigger you need to chop an inch off the engine
lifting bracket to get it in. With this done the pressure was reading as it
should. On a 3s-gte the sender is mounted right at the top of the head where the
pressure is considerably less than on the side of the block in the 4a-ge
position, with this in mind it runs roughly halfway on the gauge.
Halfway through testing on the second day and it mysteriously dropped onto 3
cylinders. Number 1 just wasn’t working, the HT lead, spark plug, injector
signal and injector resistance were all checked and found to be ok, the cam
covers were then removed and the cam shims checked along with an inspection for
a sticking inlet valve, still nothing found. Getting really worried I did a
compression test on the whole engine, I had 160 psi on 2,3 and 4 but number 1
was 70 psi…..not good! I've come across a similar problem before with an engine
that’s stood for a long time and I poured about 200ml of oil down the spark plug
hole and let it seep past the rings. Sometimes they fail to expand on an engine
that’s been standing and that’s what happened here. After cranking with ignition
disabled I soon got the Psi back up to 160 on all four and it's ran sweet ever
since. It's therefore important to get plenty of oil down the rings before
trying to start, bear in mind there will be lots of smoke! I won't know turbo
boost figures until it goes on the road but the turbo seems to be working fine,
I’ll have max bhp figures soon from its first dyno test and I'm expecting about
235 bhp…225 standard plus 10 bhp or so from the induction kit and free flow
exhaust system, then with the addition of a Blitz boost controller and an HKS
fuel cut defencer, should see it into 250 territory on about 14psi of boost. So
far the check engine light has stayed off proving my wiring is correct but it
may well come on at a later date, ECUs have literally got a mind of their own!
Other than these teething troubles the cam shims could do with replacing as the
top end is a bit tappety in places also meaning I won't be getting 100% lift on
the valves so that’s high on the list of must do jobs.
The problems I've had are relatively minor and considering this engine last
ran in a MK2 bay I think its worked out well, if there's anything I've learned
doing this it's that you can't do enough research before starting.
Turning the key for the first time....
Everything is fine
The finished installation
Project update Monday 24th November
2003:
Its one year on from the completion of the MK1 turbo project and
I’ve been asked by quite a few people recently “how’s it running?” ”have you had
any problems?” So I thought the time was right to supply an update on how it all
worked out.
Since doing the swap I’ve been blown away with the amount of interest a MK1
turbo has generated, it seems I’m not alone in wanting a car that looks like a
MK1, handles like a MK1 but has the power of the MK2 turbo. My email inbox gets
filled every week with MK1 people worldwide wanting to do the swap or having a
problem mid swap. So an update on the birthday of the UK’s first MK1 turbo seems
apt.
Since it was completed around 5 more 3sgte powered MK1s have been put into
production and earlier this year Nik Farmer from Milton Keynes rolled out UK MK1
turbo number 2 so congratulations go to him. Nik had quite a rough time with
wrong parts being sent to him, in particular the company he got the engine and
gearbox from sent him the totally wrong ECU for that engine! As if doing a MK1
turbo swap wasn’t hard enough! After trying to wire up this ECU for about a week
we discovered it was from a normally aspirated 97 model MR2, apart from that Nik
had his gearbox seize up on him which again wasn’t swap related just bad luck,
so despite all the problems he came through, well done Nik.
From the moment mine went on the road I knew I was driving something special,
it was a very weird feeling indeed sitting in a car I had owned and driven as a
daily driver for over 5 years and then feeling that turbo spool up behind my
head and feeling a huge surge of power launch it forward…the first week was the
worst, or the best depending how you look at it, half expecting something
terrible to happen and a million thoughts like “did I fasten that properly” or
“have I made that strong enough” flashing through my mind every time I squeezed
the throttle, it took over a week to build up enough confidence to find a long
straight road and open it up, quite simply doing the conversion totally changed
the driving character of this once tame little MR2.
The following weeks were amazing and driving the only MK1 turbo in the UK was
quite a buzz, it was time to enjoy those long weeks of toiled labour and head
scratching and that’s exactly what I did. The car had its first real road test
on its debut at this years JAE at Billing Aquadrome, needless to say I was very
anxious about such a long journey in an unproven car. I just took it easy all
the way there and we drove in convoy through some absolutely terrible rainstorms
which didn’t help my MK1 turbo nerves at all. Having got there all seemed well
but the following morning the car violently overheated 5 minutes after start up,
after some investigation it appeared that an 18 year old jubilee clip on the
front radiator hose had let me down and it was leaking coolant here. The MK1
members rallied round in true club style and with a jack from one member,
something to lie down on from another, cable ties and clips from Alan Jones and
a wealth of moral support from others the problem was soon sorted, what a truly
great club this is. During the show the car attracted a lot of interest and I
got rewarded for my efforts with best modified which was an honour for me given
the very high standard of the competition. With a great show under its belt we
headed off home and at the first pitstop for a hamburger there where pints of
coolant leaking out from the engine bay, it was overheating again….!! Well you
always fear the worst and thoughts of the head gasket being the culprit and
every other really nasty cause of this coolant problem were foremost in my mind,
I refilled the coolant system and limped the car home keeping on eye on the
temperature gauge the whole way! After a week of trying to stop it overheating I
was just about to strip the head off when an embarrassing phone call from Mr
Alan Jones put things in a different light…..”you have got the expansion bottle
cap on the right way round haven’t you Paul?” Yep it was as simple as that, in
doing the conversion I missed that tiny detail and it was dumping its coolant on
the floor after each run. 5 seconds after the phone call it was fixed and the
coolant system has been perfect to this day, cheers Al.
The performance during the first few months was amazing, 0-60 in just under 5
seconds and a top speed of 160mph (on a private road of course officer!)….but
with all things fast they soon seem tame again once you get used to it, and this
is what happened. In the never ending quest to go quicker and get the wow factor
back I started cranking the boost pressure up, before long it was on its fuel
cut limit at 12psi and going like a rocket. I did however find that the MR2
ct-26 turbocharger is a bit gutless over 5,500 rpm and runs out of breath and
over 6,000 rpm it just behaved like a 2ltr NA. Fate it would seem would
intervene and decide my next course of action. On the way to work one day in it
there was quite a bit of black smoke behind me and after a lot of inspection the
turbo shaft had decided enough was enough…it seems I just asked it to perform
too much in its late stage of life and as it was pumping oil into my engine it
died, I’d like to think it died a happy death but knowing that it spins at
150,000 times a minute it was probably quite violent in the end! So a new turbo
was on the shopping list and this seemed the perfect opportunity to upgrade and
give the car its “kick” back. After a week of info gathering I found that an
87-92 Supra 3.0ltr turbo has a ct-26 on it, but here’s the joyous part…that
Supra ct-26 has a much larger compressor wheel than the MR2 ct-26, within a few
days I had bought a low mileage Supra ct-26 and fitted it. While I was taking
time to fit a new turbo charger I also decided that as I was going to be running
more boost I really did need to upgrade my intercooler system as well. Again in
true Woods fashion I managed to locate a Supra twin turbo intercooler which is
basically three times the volume of an MR2 turbo intercooler. I also decided to
make the intercooler piping less restrictive and improve the flow rate.
Here’s the Supra IC in place with a vented section under it allowing it to
breath through the boot floor.
Coupled to this I planned a water injection system, not a shop bought system
but in fact one designed and made by me. The purpose of water injection on a
turbocharged engine is to reduce the high intake charge temperature and
therefore prevent any detonation that may occur, as detonation is an engine
killer so that’s the last thing we want. It also improves the density of the
intake air/fuel mixture and improves the combustion process. After experimenting
with different components I found that a Celica cold start injector provided a
nice misty spray that was going to be perfect for my water injection set up, so
I made a fitting that the injector could bolt to and then welded this fitting to
my new intercooler pipe.
The injector is mounted halfway between the intercooler and throttle body. To
supply the injector with pressurized water I’ve got a windscreen washer bottle
with an MR2 fuel pump plumbed up to it, this delivers quite a forceful supply of
water to the injector. Obviously we only need the injector to open at high boost
pressures and to control the whole system I’ve got an adjustable Hobbs 10psi
pressure switch mounted into the IC piping. This switch senses when pressure
over 10psi is reached, it switches the pump on in the reservoir and opens the
injector at the same time.
The DIY FCD in situ, maybe not very pretty but very good at its job, a bit
like me!
So with all of the new intercooler in place, the bigger turbo installed with
a Grainger valve plumbed to its actuator to raise the boost and my own brand of
water injection system coupled with my FCD design it was ready for the road once
more…I have to say I was simply shocked by the power increase from this new
turbo and my little gadgets, it feels twice as powerful as it ever did before
and its mission accomplished on the turbo upgrade! I haven’t had time to dyno it
yet but I wouldn’t be surprised if it was pushing 300bhp,im estimating around
280bhp though to be on the conservative side.0-60 is now 4.5 seconds but the
real power comes in halfway through 3rd gear, there's a huge kick of torque
right about 4,000rpm and it keeps on pulling very hard right through 4th gear
and beyond, it just doesn’t run out of puff like it used to do. My fuel economy
is absolutely shocking though but in this type of car who cares about that?
Since this upgrade I've had concerns about the gearbox not shifting from 4th
down to 3rd properly but this turned out to be nothing more than the shift cable
not secured into its bracket properly.
To monitor what’s actually going on when this happens I’ve got an Equus air
temperature probe and gauge in the system so I can tell what temperature the
intake charge is with the water injection on and off. It works really well and
I’ve found its lowering the intake charge temp by nearly 20 degrees C at full
boost which is fantastic. This in effect means I could advance the timing a
little bit more and know I’m not risking detonation.
A diagram showing my FCD design, simple yet effective.
The Supra intercooler itself is mounted in the same place the old one was but
this time I’ve cut a large hole in the boot floor and ducted the IC to this so
that the fan inside the ducting is drawing fresh cold air from the outside
world. Now that I had sufficient cooling and a fresh turbo fitted capable of
higher pressures I had to stop the Toyota management system from cutting the
fuel off at high boost. It does this via the turbo pressure sensor which will
provide the ECU with an electrical signal to inform it when 12psi is reached,
anything over 12psi and the ECU kills the fuel injectors and all power is lost
until boost has gone away. It’s a very good system designed to protect the
engine should a problem occur with the actuator or its hoses or even the turbo
itself, but it’s a total killjoy when we want to boost higher than 12psi. In
this respect an FCD (Fuel Cut Defender) must be used to fool the ECU into
thinking less than 12psi is being made even when 15 psi is produced by the
turbo. Now FCDs are readily available but you know me and I’d rather design and
make one of my own than buy one…so I did! The problem with most FCDs is that
they either get rid of the fuel cut off altogether which does prevent fuel cut
from happening but the downside is zero protection, so I had to come up with a
system that still kept the protection level only raising it to whatever limit I
liked. After playing around with some bleed valves and some vsv’s I came up with
my own design of FCD that raises the cut off point pneumatically and still gives
engine protection.
Water injection reservoir and MR2 fuel pump deliver pressurized water to the
injector on the intercooler pipe
One of the big successes with the project was the brake conversion… www.mr2mk1club.com/Bigbrakes.html
its definitely needed lets put it that way and the only problem I’ve had with it
is a squealing pad on the left front but that teaches me for using cheap pads
instead of paying that little bit more and getting quality ones, lesson learnt!
It stops like its hit a wall, totally amazing brakes on those GT4s and I know
why they use them now, I was concerned about there being no engine weight above
the front brakes like there is on a GT4 but this hasn’t proved significant and
it only ever locks up when you mash the pedal to the floor violently, quite
simply it couldn’t have worked out better in the braking department.
In all I’ve had no more problems with the MK1 turbo than the average MK2
turbo owner has, and certainly there have been no swap related problems (apart
from me fitting the expansion cap on back to front) ie. No part of the engines
installation into a MK1 has affected how it runs or behaves so I’m quite pleased
with that as I was expecting there to be bugs to iron out. The whole project has
been a vast learning curve as other MK1 turbo swappers are now finding out and
if I had to do it all again I would, there are a few things I may have done
differently though, one of these would be totally rebuilding the 3s-gte engine
before fitment as its quite hard to do work on it given the space limitations.
Another would be possibly doing it to a supercharger model as they have tougher
chassis and better bodywork in general. As Nik and anyone else who has driven a
3s-gte powered MK1 will agree, there’s nothing that compares to it, ok its far
from the fastest car on the road but part of the feeling is knowing that you are
driving a car that wasn’t meant to be….I’ve often wondered what Toyotas version
would have looked like if they had made a 2ltr MK1 turbo?
Nik Farmers recently completed turbo
A few weeks ago I did consider selling the MK1 on to make way for the next
big project but every time I drive the car it just makes me smile and not many
cars can do that, so its staying for the foreseeable future. This won’t deter
the next project though which will offer the same power delivery as the 3s-gte
without the turbo. I’m going to build a V6 MK1, the engine I’m going to use is
from the Toyota Camry 3.0ltr V6 1MZ-FE, its an all aluminium block and very
light for the size of the engine, in fact it only weighs a few kilos more than
the 4a-ge! This swap has been done before in the States to a MK1 so I know it
fits. Its got to be mated to an MR2 turbo E153 gearbox and a few engine mounts
made etc. but nothing amazing. A full step by step article on this site will
accompany that project just like the MK1 turbo.
PAUL WOODS paulwoods.v6mr2@ukf.net
Project update Thursday 14th November 2002: